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Yaskawa SGMPH-08AAA-SE41 AC Servo Motor Hauptbild
16.06.2026 by Viktor Siebert
Repair of a Yaskawa SGMPH-08AAA-SE41 AC Servo Motor after Encoder Failure Caused by Coolant Ingress in a Star CNC Machine

A few weeks ago, we received a Yaskawa SGMPH-08AAA-SE41 AC Servo Motor from a Star Swiss-type lathe for inspection and repair. The motor was operating together with a Yaskawa SGDK-101010AEA-VY24 Servopack in a machine equipped with Siemens and Yaskawa control technology.

The customer reported sporadic positioning errors and unstable axis behavior. The machine was operating in an environment exposed to coolant and emulsion. Since the system was required for ongoing production, there was considerable time pressure to identify the cause quickly and implement a sustainable repair.

Initial Diagnosis

During the incoming inspection, it became apparent that the motor showed clear signs of moisture ingress.

After disassembly, the following findings were identified:

• Age-related deterioration of shaft seals

• Coolant and emulsion ingress into the motor housing

• Moisture and corrosion traces inside the encoder compartment

• Contamination of sensor elements and electrical connectors

• Early-stage oxidation of components within the feedback system

The mechanical components of the motor were still in good condition. However, the encoder had been significantly affected by the coolant contamination.

Root Cause Analysis

The technical investigation revealed the following chain of events:

• Worn shaft seals lost their protective capability

• Coolant and emulsion entered the motor housing

• The UTSIH-B13DC-E encoder became contaminated by moisture

• Position feedback signals became unstable

• The axis control system could no longer process reliable feedback data

• Initial positioning deviations and operational faults occurred

The motor itself was not the root cause of the failure. The damage was caused by progressive seal deterioration and the resulting contamination of the encoder system.

Repair Measures

Our technicians carried out the following work:

• Complete disassembly of the motor

• Removal of all coolant and emulsion residues

• Cleaning of stator, rotor and housing

• Drying of all components

• Inspection of all motor windings

• Repair and restoration of the UTSIH-B13DC-E encoder

• Replacement of all seals

• Preventive replacement of bearings

• Inspection of all connectors

• Encoder realignment and calibration

• Surface refinishing and final cleaning

After completion of the repair, the motor was reassembled and fully tested.

Final Testing and Return to Customer

The motor was tested on our test bench together with a Yaskawa SGDK-101010AEA-VY24 Servopack. Encoder feedback signals were monitored throughout the complete speed range.

The following tests were performed:

• Encoder functionality

• Positioning accuracy

• Speed performance

• Signal quality

• Temperature behavior

• Long-term stability

After successful completion of all tests, the motor was approved for return shipment.

Customer Feedback

“Thank you for the quick repair. After installation, the axis is operating reliably again and all positioning errors have disappeared.”

formation about the mentioned Servomotor and other components:

Yaskawa SGMPH-08AAA-SE41 AC Servo Motor

More information about our Yaskawa repairs can be found here.

📞 Feel free to contact us if you have any questions regarding your Yaskawa drive

Technical Specifications

SpecificationValue
ManufacturerYaskawa
ModelSGMPH-08AAA-SE41
Motor SeriesSGMPH
Motor TypeAC Servo Motor
Rated Power750 W
Rated Voltage200 V
Rated Current5.1 A
Rated Torque1.20 Nm
Rated Speed6000 min⁻¹
EncoderUTSIH-B13DC-E
ServopackSGDK-101010AEA-VY24
Machine ApplicationStar Swiss-Type Lathe
Drive MethodDirect Drive

The values are taken directly from the motor nameplate.

Operating Conditions

ParameterValue
Ambient Temperature0 to +40 °C
Storage Temperature-20 to +60 °C
Humidity20 to 80 %, non-condensing
Liquid ProtectionFunctional seals required
Mounting MethodFlange mounted
Application EnvironmentCNC machines, machine tools
Drive MethodDirect drive

The general operating conditions correspond to Yaskawa M, F, S and D Series servo systems.

Integration with Other Equipment

The motor was used together with:

• Yaskawa SGDK-101010AEA-VY24 Servopack

• Siemens CNC control system

• Star Swiss-type lathe

• Yaskawa UTSIH-B13DC-E feedback system

• Yaskawa servo drive system

Functional Description

The SGMPH-08AAA-SE41 is a high-dynamic AC servo motor designed for precise positioning tasks in CNC applications.

The Servopack processes machine control commands and regulates torque, speed and position. The UTSIH-B13DC-E encoder continuously provides position feedback data required for closed-loop control.

This allows:

• High positioning accuracy

• Fast dynamic response

• Excellent control stability

• Precise axis movements

• Reliable monitoring of speed and position

The Yaskawa servo system uses continuous encoder feedback to regulate motor performance at all times.

Alarm and Error Codes

The following alarms may occur in servo systems based on the uploaded Yaskawa alarm documentation.

AlarmError NameDescriptionResetCorrective Action
0x10Over CurrentExcessive motor currentYesCheck motor and wiring
0x11Ground FaultGround leakage detectedYesCheck insulation
0x20Fuse Blow-OutInternal fuse failureYesInspect power section
0x40Over VoltageExcessive supply voltageYesCheck incoming power
0x41Low VoltageSupply voltage too lowYesCheck power supply
0x51Over SpeedExcessive motor speedYesCheck encoder and parameters
0x79Motor OverheatMotor temperature too highYesCheck cooling and load
0x81PG Backup ErrorEncoder backup faultYesCheck encoder
0x85PG Over SpeedEncoder overspeed faultYesCheck feedback system
0xC9PG Communication ErrorEncoder communication faultYesCheck encoder cable and encoder

The alarm table is based on the uploaded Yaskawa servo alarm documentation.

Preventive Measures for the Customer

MeasureRecommendation
Inspect sealsRegularly check for wear and damage
Monitor coolant systemAvoid direct coolant contact with motors
Inspect connectorsClean during scheduled maintenance
Check encoder areaMonitor for moisture and corrosion
Monitor bearingsCheck noise and running condition
Clean motor exteriorRemove dirt and contamination regularly

Conclusion

This repair case demonstrates that servo motor failures are not always caused by electrical defects. In this Yaskawa SGMPH-08AAA-SE41 servo motor, aged shaft seals allowed coolant and emulsion to enter the motor housing. As a result, the UTSIH-B13DC-E encoder was damaged and reliable position feedback was no longer possible.

By repairing the encoder, replacing all seals, carrying out preventive bearing replacement and performing precise encoder calibration, the motor was successfully restored to full functionality and is now ready for many more years of reliable operation.

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