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24.02.2026 by Viktor Siebert
Repair of a Mitsubishi AC Servo Motor HF-H154BS after emulsion damage with insulation failure and encoder defect

Initial Situation and Fault Pattern.

The Mitsubishi HF-H154BS AC servo motor was operated together with an MDS-DH-V2-2020 servo drive unit. According to the customer, increasing operational faults occurred. The motor could no longer be referenced reliably, the holding brake no longer opened and closed correctly and insulation problems appeared.

Upon arrival, the overall condition was clearly damaged. The insulation values of the stator were far below the nominal range. In addition, the holding brake showed electrical abnormalities and had no defined mechanical function. The encoder was contaminated with emulsion. The bearings showed increased play and running noise.

Technically noticeable was the combination of poor insulation, encoder failure and mechanical stiffness. The relationship between operating action and fault was clear: after switching on, unstable control behavior occurred, especially at low speed and during positioning movements.

Incoming Inspection and Initial Diagnosis

The first step was visual inspection. Emulsion residue was visible in the area of the encoder, brake and winding head. The seals were hardened and no longer sealing.

Insulation measurement between winding and housing showed values clearly below 1 MOhm at 500 VDC. Safe operation was therefore impossible.

The encoder no longer delivered a plausible signal. The brake did not energize reliably. Mechanically the shaft could only be rotated stiffly, indicating worn bearings.

Technical Analysis

The cause effect chain was clear. Due to damaged seals, emulsion entered the motor housing. This conductive liquid led to leakage currents in the winding area. As a result, insulation values dropped drastically.

In the encoder area, moisture caused corrosion and signal disturbances. The feedback signal became implausible. The control system could no longer position stably, especially at low speed.

In the holding brake area, the emulsion caused corrosion and mechanical sticking. As a result, mechanical functionality was no longer ensured.

The bearings showed grease loss and corrosion marks due to fluid ingress. The increased play additionally affected control behavior negatively.

Such damage patterns are typical for aging seals combined with aggressive coolant environments.

Repair Measures and Overhaul

Due to the moisture damage, partial repair was not reasonable. The encoder was mechanically and electrically damaged. Stable repair of individual components would not have been sustainable.

Performed actions:

  • Complete replacement of feedback unit
  • Replacement of holding brake
  • Replacement of all bearings
  • Renewal of all seals
  • Cleaning and drying of stator area
  • Insulation test after cleaning
  • Signal quality test after encoder replacement

All connection cables and connectors were checked. Thermal monitoring was simulated on the test bench.

As a preventive measure, the sealing concept was improved and regular inspection of sealing areas was recommended to the customer.

Final Functional Test

The functional test was performed on a test bench with an MDS-DH-V2-2020 drive unit.

Tested:

  • On off behavior
  • Referencing
  • Positioning at low speed
  • Speed ramp up to nominal speed
  • Thermal stability
  • Overcurrent and signal monitoring

The motor ran vibration free, reproducible and without fault messages. Insulation values were again above 100 MOhm at 500 VDC.

The brake opened and closed within specification.

Conclusion

The damage was clearly caused by emulsion ingress. By completely replacing all affected assemblies, operational safety was restored.

Partial repair would not have delivered a stable long term result. The performed overhaul represents a sustainable solution and significantly increases machine availability.

To mentioned Mitsubishi Motor:

Mitsubishi HF-H154BS AC Servo Motor

More details about our Mitsubishi repair services can be found here:
Mitsubishi motor Repair by Industrypart

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Technical Specifications

FeatureValue
ManufacturerMitsubishi Electric
Device TypeAC Servo Motor
ModelHF-H154BS
SeriesHF Series
Power1.5 kW
Input Voltageapprox. 3AC 348 V
Output Voltageapprox. 200 V class
Rated Currentapprox. 2.7 A
Control TypeSpeed and position control
FeedbackIncremental encoder Mitsubishi OSA18-100
CoolingSelf cooled
Protection ClassIP67
Ambient Temperature0 to 40 °C
MountingFlange mounting
OriginMade in Japan
Product StatusActive

Application Environment and Compatibility

Typical applications:

  • CNC machining centers
  • Machine tools
  • Automation systems
  • Positioning axes

Typical production years: approx. 2005 to 2015

Requirements:

  • Dry environment or protected installation
  • Clean cable routing
  • Stable voltage supply
  • Protection against coolant

Functional Description

The motor operates as a permanent magnet synchronous motor. Power control is provided by the MDS-DH-V2-2020 servo drive.

Feedback supplies position and speed information. Closed loop control is implemented.

Protection functions:

  • Overcurrent monitoring
  • Temperature monitoring
  • Feedback signal monitoring
  • Insulation protection

These functions are safety relevant for precise positioning.

Alarm Messages and Troubleshooting

Based on Alarme

Alarm CodeDescriptionPossible CauseAction
10Insufficient voltageVoltage dropCheck supply
17A/D converter errorCurrent feedback errorCheck drive
24GroundingMotor to ground faultMeasure insulation
30Over regenerationBrake resistor overloadCheck resistor
31OverspeedSpeed exceededCheck parameters
32Power module overcurrentPower stage overloadCheck motor
33OvervoltageDC bus too highCheck supply
46Motor overheatTemperature too highCheck cooling
50Overload 1Motor overloadReduce load
51Overload 2Continuous high currentCheck parameters

Assembly Overview

AssemblyDescriptionFunctionNotes
StatorWinding unitTorque generationCheck insulation
RotorPermanent magnet unitMagnetic fieldMechanical check
FeedbackIncremental encoderPosition feedbackCheck signal
Holding brake24 V DC brakeHolding functionCheck switching time
BearingsShaft bearingsMechanical guidanceCheck play
Sealing systemShaft sealProtection against fluidRegular inspection

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